- Joined
- Dec 25, 2002
- Location
- mont, AL
bhg confirmed, distorted around #3. I think age and rot contributed to the failure, and it was juuust barely blown. pistons all still look mostly good, chambers look good, just a little color difference on the #3 plug. compression numbers across the board were still good, etc etc.
head was a bit crusty coming apart, I may do some pre-cleaning before I cart it to the machine shop for a skim and a valve job. checked lash with the ipd turbo cam, everything (For the most part) is a touch loose cold, need to compare that with the cam that was in there (T) and see if things remain consistent, that'll make the swaprooskie work a bit easier. either way I'll get it set up for the ipd cam since that's what's going to get stuffed in there shortly after it goes back together.
head was a bit crusty coming apart, I may do some pre-cleaning before I cart it to the machine shop for a skim and a valve job. checked lash with the ipd turbo cam, everything (For the most part) is a touch loose cold, need to compare that with the cam that was in there (T) and see if things remain consistent, that'll make the swaprooskie work a bit easier. either way I'll get it set up for the ipd cam since that's what's going to get stuffed in there shortly after it goes back together.