rb92673
racecar
- Joined
- Jan 17, 2017
- Location
- San Clemente
I thought I would start documenting my POS Lemons car. This forum has been very helpful to me along this journey.
So I bought this 85 745 with B230FT in 2017 to race 24 Hours of Lemons (24HoL). I had originally planned to build a 84 760T that my dad let sit in his backyard since about 1988, but this car was already caged and was almost ready to go.
Car was basic 1985 745T. It had a stock T3 turbo, cut springs and that was about it.
Wiring was in bad shape. Car did not run.
I didn?t really have much experience with wiring or anything outside of basic DIY car stuff. Brakes, changing shocks/springs, exhaust swap out, etc. I found a green book for wiring and started labeling and tracing everything. Since this is a race car and will never see street use again, I started removing unnecessary wiring to make it easier to troubleshoot.
After a while I found things like a missing over-boost switch, fuel pumps wired incorrectly, stuff just disconnected, etc. and it fired up. Seemed to idle and run pretty good, but was running pretty rich. A new FPR and I was ready for a track day to shake it down.
After a few 20 minute sessions on track it had developed an exhaust leak.
Three studs on the turbo had backed out then sheared off.
These were too far to drill out so I found a shop in Santa Ana, CA that burned them out. Jerry?s Broken Drill and Tap Removal. http://brokentap.com/
I replaced the hardware with nice locking nuts and new studs and thought we would be good. Little did I know, but we would have the same exact problem at our first race 24HoL Button Terrible Sept 2017. We didn?t break any studs, but we did lose a couple.
We managed to finish the race, even with a couple hours off track for some repairs. We did have an intermittent power loss that would occur in some corners, we traced it down to a bad splice in the hall sensor shielded wire after the race. Suspension was sloppy, we would find out later the shocks were completely blown out and we were basically just racing on springs.
After the race I removed the engine wiring harness and double checked every wire end to end and made necessary repairs. I also safety wired every stud between the turbo and downpipe.
So I bought this 85 745 with B230FT in 2017 to race 24 Hours of Lemons (24HoL). I had originally planned to build a 84 760T that my dad let sit in his backyard since about 1988, but this car was already caged and was almost ready to go.
Car was basic 1985 745T. It had a stock T3 turbo, cut springs and that was about it.
Wiring was in bad shape. Car did not run.
I didn?t really have much experience with wiring or anything outside of basic DIY car stuff. Brakes, changing shocks/springs, exhaust swap out, etc. I found a green book for wiring and started labeling and tracing everything. Since this is a race car and will never see street use again, I started removing unnecessary wiring to make it easier to troubleshoot.
After a while I found things like a missing over-boost switch, fuel pumps wired incorrectly, stuff just disconnected, etc. and it fired up. Seemed to idle and run pretty good, but was running pretty rich. A new FPR and I was ready for a track day to shake it down.
After a few 20 minute sessions on track it had developed an exhaust leak.
Three studs on the turbo had backed out then sheared off.
These were too far to drill out so I found a shop in Santa Ana, CA that burned them out. Jerry?s Broken Drill and Tap Removal. http://brokentap.com/
I replaced the hardware with nice locking nuts and new studs and thought we would be good. Little did I know, but we would have the same exact problem at our first race 24HoL Button Terrible Sept 2017. We didn?t break any studs, but we did lose a couple.
We managed to finish the race, even with a couple hours off track for some repairs. We did have an intermittent power loss that would occur in some corners, we traced it down to a bad splice in the hall sensor shielded wire after the race. Suspension was sloppy, we would find out later the shocks were completely blown out and we were basically just racing on springs.
After the race I removed the engine wiring harness and double checked every wire end to end and made necessary repairs. I also safety wired every stud between the turbo and downpipe.
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